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   aerothermodynamic off-design performance study of a fixed double bypass duct turbofan engine  
   
نویسنده lekzian elyas ,farshi fasih hamidreza ,modanlou reza
منبع بيستمين كنفرانس ملي ديناميك شاره ها - 1402 - دوره : 20 - بیستمین کنفرانس ملی دینامیک شاره ها - کد همایش: 02230-20410 - صفحه:0 -0
چکیده    In this paper, a turbofan engine with double bypass duct (dbp) was studied at design point and off-design conditions. this engine is a separate exhaust, two spool turbofan engine with bleed, turbine cooling, power extraction, and convergent exhaust nozzles. bypass ratio of main and secondary duct is equal one. also, a typical turbofan engine with one bypass duct is considered as the benchmark case (simple engine) and its bypass ratio is 2. simulation results show that dbp engine produces 5.4% thrust more than the simple engine at m=0.8 and altitude of 9296.4 m (design point). dbp engine thrust is more than the simple engine at sl altitude and 9296.4 m at off-design conditions in all flight mach numbers ranging from 0 to 0.8. moreover, the double bypass duct engine sfc is lower than the simple engine at prementioned off-design conditions. thrust per mass flow rate (f/m ̇) was also studied. by increasing f/m ̇, specific fuel consumption is decreased for both engine types. another interesting finding is that at constant f/m ̇, dbp engine sfc is lower than simple engine at all flight altitudes.
کلیدواژه turbofan engine ,double bypass duct ,off-design ,thrust ,specific fuel consumption.
آدرس , iran, , iran, , iran
پست الکترونیکی reza.modanloo@semnan.ac.ir
 
     
   
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